January 7th, I headed down with Thor and a truck load of gear. Had a
nice stop south of Nashville
and then drove to St Augustine in a 32 degree rain through much of
Georgia. Little did I know at the time, but I had put Thor's dish on
top of the truck as I was loading things in the rain, and I forgot
it there. It rode the whole way down to St Augustine, a healthy 750
miles or more! Saw two massive wrecks on the way down, lucky both
were for Northbound traffic. One 30 miles North of Atlanta, blocking
all three lanes of 75, and one 40 miles south of Atlanta blocking
all 4 lanes of northbound 75. The backups were huge and it would
have added a day to my trip for sure if I was going the other way.
Jan 8th, Made the rest of the drive down, racing the clock at the
end as I arrived in St Augustine at 4:50, right before the yard
closed so I was able to get in and unload the truck before spending
a not so nice night at
the local Days Inn. Not a great smelling room, not very clean, and
with some nasty bugs but they allowed Thor.
January 9th through the 15th were spent working full time on getting
the boat ready. The first few days it was just Thor and I and he hung out in the car,
after deciding my ramp was not
going to work for him.
Got a good deal done on the 9th, cleaned the cockpit, and decks, put
out cockpit cushions, helm shade, got mainsail up on top deck and
out of cabin, and dingy engine on dingy and out of cabin, fix two
spots on stern rub rail that were bulging, ran engines, filled the
water tanks and generally got things rolling. Rain held off all day
which was nice, but it did rain over night.
January 10th I move the truck under the boat so Thor could use the
back with the hatch open. This was handy as it rained hard all day. I
spent the entire day working on the instrument wiring and ended
the day with the new B&G
display mounted, the AIS installed and the radar wires pulled to
the display, so everything was now working. At 2am that night I
heard some noise in the cockpit and I knew someone was on the boat.
I bravely looked out to see what was going on and I scared a cat or
a raccoon out of the cockpit. It had been going after the garbage
bag I left in the cockpit. I also helped out a neighbors boat when
they asked me to check if their fridge was still on and if the solar
was keeping up. It was not, and the job of emptying the fridges and
freezer was a stinky one! We met them when they were
working on the boat in November getting ready, but home issues and
engine issues changed their launch date. The still had not launched
Feb 15th after numerous repairs had not fixed one engine and so they
had ordered a new one and new saildrive. Such is the cruising life I
guess... The new engine arrived on Feb 15th so hopefully they are
off an running in a few weeks.
I Spent most of the day on the 11th cleaning the hulls and then
picking things up and trying to reduce the clutter so it would look
OK when I picked up Cheryl, but the clutter was still fairly
overwhelming when she arrived as there was still a good deal of gear
to install, and the boat needed serious cleaning. It is hard to
describe the effects of 9 months of humidity, a hurricane, and the
Florida sun can have on a boat. It makes everything dirty and the
next 4 days were spent bringing the boat back to a very nice state
of clean, virtually all this work done by Cheryl.
We launched around 3PM with a makeshift "crawler",
they used the large fork lift instead. It was an interesting
process, and it went smoothly except for rubbing against the pilings
which caused some grime stains I had to wax out. It was nice to be floating, and I
fired up the dingy and gave Thor what would be the first of many, many dingy rides
over the next three months (we seem to consume about 5 gallons of
outboard fuel a week on the trip, which shows the dingy usage to get
Thor to shore). That night I got Cheryl at the airport. The number
of still uninstalled systems was a little more than she hoped for,
but, as always, she took it in stride.
On the 12th, Cheryl started cleaning in earnest and I worked on the
AIS antenna mount and also attacked the non-working main AC unit. I
switched out the control units and it worked, so I ordered a new
control. After I did that, the unit failed again. Some more
debugging and a call to the regional dealer lead me to a corroded
connection which was fine after some cleaning. Now I have a spare
controller... Also filled the propane tanks, sorted out the long
term parking Garage for the truck, and got more supplies. We bought
supplies each day, keeping the local economy running well! The boat
looked nice on the dock.
It was a nice way to spend
my birthday, hanging out with Cheryl, on a boat, in the water.
Plus the cooler temps made for good working conditions compared to
the heat I saw over the summer visits.
On the 13th we mounted the 3 new 100Watt solar
panels on the top of the helm station (this shot shows it a
few weeks later), mounted the controller in the nav
station, and put the SSB gear in place, but not mounted,
washed all sheets and towels, aired the boat out as it was a nice
sunny day, and did lots
more cleaning.
Starting to make a real dent, on the 14th I got the solar and SSB
power wired to the main ships power with a stand alone fuse box,
replaced the starboard engine starter, fuel filters on both engines
and did some more cleaning. I also figured out why the port aft head
motor seemed hit or miss... They had spliced the power line with a few wraps, no physical
connectors, just corroded wires.. I fixed this and it was back to
running well.
We were going to leave on the 15th, but having power for the cold
nights and water for cleaning was nice so we decided to sit one more
day. This worked out as I decided to put the new mainsail cover on
and discovered the bolt rope holding it into the boom was too small
and would not work. Some quick thinking and we had the new and old
covers at the Irish Sail Lady for a fix. Hope to pick it up late on
the 16th.
With the mainsail work on hold, I took the fuel level sender out of
the port tank and after taking it entirely apart, I managed to get
it back working, so now we have functioning fuel gauges on both
tanks. Also took the opportunity to do some test runs in the dingy.
It seems to have managed the summer just fine and my "stabil" gas
from the BVI still seems to be doing the trick. Next storage period
I think I will go with full fuel and water tanks as it is handy to
have water when you visit. We get the guest cabin ready for
the first visitor of 2018...
One the 16th we headed out..... On the road to adventure.
Kathy comes and we grab a can to meet her in St Augustine. Fuel
1/4 Star, 3/8 Port. Star head is locked up, motor is frozen, and I
could not get the parts out of the base. I gave it a good try
though, and the base broke. Need
to get a new base which we ordered for delivery in Cape
Canaveral in a few days..
Picked up the mainsail cover (thanks to Kathy), and moved the truck
to the garage. Cold night of 40 degrees.
17th worked on both engine belts, tightened them, but they do not
stay tight. This was to turn out to be a multi week issue, finally
traced to the Yanmar belts and rust on the pulleys for the belt.
Wire brushed and clean fuel bowl so it would not loose pressure on
port engine. Seemed to solve issues. Also put on mainsail cover and
main, without the battens. Pretty tough job. But got it off the
deck. Met up with Tony and Mary and had a very nice visit. Saw lots
of Dolphin in the harbor and around the dingy docks which was nice.
Very cold temps with lows
of 28 degrees at night. Thor's dish had ice over the top of it. The
fresh water pump runs on occasion, and we are not sure where the
issue is. We later trace it down to a cracked filter bowl. My guess
is it cracked in the freeze we had a couple of weeks before
launching the boat. Fun to be out
of the Wisconsin cold !
18th Drop Kathy off at 7:30am. She got to the airport early,
but her flight was messed up. Had 6 hours of delays. Windy day. We
work on the heads some and more cleaning. Based on weather, we
decide punching down is a good plan, so we skip Daytona beach.
19th After 7 days on the holding tanks, we are off to the ocean. We
fill tanks. 57 gals in port tank, (was 1/4 full) and 45 gals in Star
tank (also showing 1/4 full). This replaces the Fuel John and I used
bringing the boat back from Puerto Rico in April last year. We carry
180 gallons of fuel, 90 in each tank. We also got 4 gallons of gas
to add to the 5 gallons we bought in St Augustine gas stations). We
ran down on Star engine roughly 19 hours of run time. We left around
3:30, after smooth docking at the gas dock (I was compared to Capt
Ron, which is something of a docking compliment if you ever saw the
movie). It was a calm and cool night, Thor was a little nervous
about the whole thing.
20th We arrive in Cape Canaveral around 10am and go through the locks and the
bridge. Anchor just past the locks and play on a couple of tiny little islands.
Thor got to play and swim. did not drink too much water, which was
good.
Spent afternoon mounting Starboard hatch over the aft bunk. A real
pain.
21st took a long dingy ride and a modest break from cleaning and
work. Ran 3.5 miles down the canal between the rivers. The other big
project was wiring up the glass
solar panels and cleaning
up the wiring. We jury rigged a tv antenna and watched the
Vikes get killed by the Eagles in the NFC championship game.
Monday Jan 22, we moved over to Ocean Club Marina in Cape
Canaveral. A very nice spot, where we met up with James and Jill. I
took the new base and rebuilt
the star aft head while the rest of the gang got groceries and
sorted out parking the camper. We enjoyed a nice dinner ashore
courtesy of Jill and James.
Jan 23, we spent most of the day at the Space museum, it was a very
interesting tour and a fun place to check out. Tasty burger at the
Orbit Cafe.
Jan 24 we head out around 1PM, and sailed the rest of the day and
that night in a building North breeze. It ends up blowing around
20-25 from the North, and we run down under just the Genoa (knocking
the mainsail before dark). Very pleasant sail, and with a full crew,
the watches were easy.
25th, we got there a little too early and we looped for 30 minutes
to get a little more sunrise going. The Star engine gave up a water
alarm in the sail drive, so we just used the port engine. Turned out
the alarm was false, but did give us some practice maneuvering under
one engine. This was the start of a series of engine issues with the
sail drives...
We anchor in the "north anchorage" of lake worth, and enjoy pretty
good protection from the windy days that follow. John is holed up in
Bimini with a slip for a month waiting out the weather. Blowing
steady 20-25, but Mantus holds like a champ, and Anchor hook rope
works great. Thor enjoys
the first of many trips to Peanut Island, where we can dump
trash and generally get him off the boat.
26th The generator was slow starting so we took new battery from
port engine and gave it to the generator. The Generator has glow
plugs so it has the toughest start loads. Also wire brushed the
negative leads. Found a broken hose clamp on the generator exhaust
line as well.
27th, James and Jill head out in the morning and we replace the port aft hatch.
Always a pain as the nuts are very hard to get at, and the hatch
takes 2 hours of wedging and cutting and prying to get off once the
crews are out. Not something I hope to do again, but the new hatch looks great,
and a critical leak is gone from the boat.
We ran Thor some, and left the lease on. He tripped on the leash and
took a nasty fall on the road at Peanut Island. Cut up his feet some
and broke a toe nail, but looked worse. He is a trooper, so we hate
to see this happen. He recovers smoothly from this spill, and as
always, takes the whole thing in stride.
There are four Cats anchored nearby, and they invited us over for
happy hour tonight. It is interesting to hear everyone’s plans and
they are also looking for a weather window to either head to the
Bahamas or in one case, head down towards south America.
28th discovered AIS not transmitting, not getting a GPS signal
apparently. I ordered an antenna for the kids to bring down
hopefully this will fix it. Paul visited the boat and checked things
out. It was nice to see him and get him on the boat. Made an effort
to organize and pick up tools and half way install the inverter.
Spend time each day on Peanut
Island walking Thor (3 times a day). It is a fairly sloppy
dingy ride over, but good for the dog and easy access. We sometimes
see manatees and Dolphins
which is cool. The Manatees
hang out in a little basin where we could dock the dingy if we
did not like the beach that day.
1/29 saw Steve Jobs boat
drift by, he had commissioned it, but it was not finished
before he died. I also worked on PSP taxes as they need to be filed
by March 15th and we will not be home yet... Running a business from
the boat is always tricky :-). We upped anchor, headed out into the
Ocean and pumped the heads, and tested the new alternator belts I
had installed on each engine. The belts were very hard to get on,
needed a screw driver to wedge them over the pulleys, but they
loosen up when running. I need to find a way to get more
tension on the alternator arm bolts. Still mainly working on the
boat and troubleshooting things every day. We also noticed the port
sail drive was very
full with oil, which indicates a prop seal leak and water
getting into the drive... More fun! I drain out 1 quart of oil and
add fresh oil. After a few tests, it seems we may have a slow leak,
so this will be something to keep an eye on.
1/30 Replaced the bow port side hatch screen. Tried to replace the
starboard aft screen as well, but discovered the headliner boards
needed to be epoxied up to
the deck before the screen could be installed correctly. Set
the Epoxy and will install the screen tomorrow. Very windy 25-30 knots all
day. One more day of working all day on the engines and sorting out
other items. We lose the board that closes off the battery box
overboard as it takes a flying leap off the tramp in the bow during
a gust. Cheryl and I are too lazy or whatever to dive in and get
it... Lucky our boys are tougher.
1/31 Wed, we upped anchor and motored a few miles south on the ICW,
stopping at Palm Harbor
Marina (a real super yacht marina,with many large and cool
boats.) We filled the water tanks (down about 120 gals I would say),
and put 13.6 gals of fuel in Star tank, gauge read 3/4. Also picked
up 9 gallons of gas. anchored between the bridges and went ashore to
get some food supplies. Later went in and had a nice dinner.
Had a small mistake anchoring as there was current and I thought the
boat was not moving, but we were dropping back at 2knots with the
current. Put a lot of strain on the windlass when we pulled tight. I
will feather out the bridal retrieval line from now on... Did get
the hatch screen
installed, overall a good day.
Pretty night in a pretty spot.
2/1 Thurs We continue to fix things here and there on the
boat, and a few of them are interesting (code for a less pleasant
phrase :-)
One such issue I have been fighting the last week has been
alternator belts getting chewed to bits over a few hours of engine
run time. I had decided this was because I could not keep tension in
the belts, and I came up with a number of clever and drastic ways to
keep the belt from loosing tension. Over a few days, and some
internet research (since my tension ideas all seemed to fail
miserably), I discovered the cause was rust on the engine and
alternator pulleys. This rust was eating the belt, causing it to get thinner, hence ride
lower in the groves and become looser. I will work on this theory
once I can get new belts.
We motored back to our old spot to pick up the boys and Diana
tonight late.
Poked around and bought them a parking pass, as they do not let cars
in the lot overnight here. Hung a couple of the blinds Cheryl made
and discovered the star sail drive water sensor was broken (so had
to disconnect it), and also discovered the Port engine heater hose
was cut at the pipe right above the alternator. It would leak if I
lifted it up, the hatch latch over the alternator also leaked.. No
wonder the pulleys were rusting. I cut the hose shorter and
re-attached it, and had earlier rebedded the latch fitting. Should
be much drier now. Need to get new hoses run as the old ones show
some wear. Much calmer night wind wise, which will make picking up
the kids easier.
2/2 Friday
Picked up the kids at 1:30am. Smooth dingy ride out to the boat,
although it was Diana's first dingy ride, which had to be fun in the
middle of the night. In the morning, Cheryl got some groceries and
when I was restocking the beer, I discovered where the leak was in
the water system. The filter bowl was leaking, likely cracked in the
hard freeze a few weeks before we launched. After some futzing, I
resealed the bowl with boat life caulk, which helped a lot, but
there was still a small leak. After this fun, we had a great sail with a
nice 12-15 knot wind and pretty
smooth ocean. Also mounted the AIS GPS antenna Matthew brought
down and this all seemed to work, so now the AIS is back in
business.
2/3 We anchored right where we had a few days earlier when the wind
blew the battery door over the side. We saw the door in the water
next to the boat, and Matthew kindly agreed to dive in and grab it,
which he managed on the first dive. Since it was still windy, after
a walk on peanut island, we moved the boat a few miles so we could have a nice dinner
without getting wet. The boys treated and it was great!
2/4 The kids had to leave around 12:30 so we moved back to the old
spot and had a smooth drop off, without anyone getting wet, despite
the strong breeze. It was behind us going in, Cheryl and I got wet
coming back out!
2/5 Monday, headed out to Ft Lauderdale, leaving around 4:30am. It
is a real zoo in Ft Lauderdale, and we have a few problem boats as
we wait for the bridge. We get in smoothly and dock into a tight spot
with surprising smoothness and skill (surprising to me anyway). We
did 6 loads of laundry, got a car, called in a prescription and
washed down the boat before meeting up with a long time work
colleague Bob VanValzah and his wife Eileen for drinks and dinner
around 4.
2/6 Tuesday was our re provision day and we used it fully. From food
to parts to fix the water system, to new alternator belts, we got it
all, and returned the car on time. I spent the morning while Cheryl
got food sanding all the pulleys on the port engine (the rust was shredding the belts).
I put on the new NAPA belt, which was so tight I had to pull the
water pump pulley off and reassemble it with the belt on, and things
seem solid. This seemed to fix the problem, so I will need to do it
on the Starboard engine as well. I cleaned up the belt dust and
fragments, and also checked the sail drive oil. The sail drive does
not seem to be letting much water in which is great. Also swapped
out the water strainer for the fresh water pump which was cracked
with a straight pipe
solution of my own design... This seemed to fix the fresh
water leak. I have a new strainer on order and should be able to go
back to the original design without too much trouble. Now I also
have a way to plumb in a replacement pump if this one ever fails.
A hard work day was capped off by a nice dinner at Paul and Lori's
wonderful house.
2/7 We head out around 9:30 and have a sloppy and windy sail down
the coast to Biscayne bay. ESE winds over 20 knots and 6 foot head
on then beam on seas make Thor and Cheryl unhappy. Thor seems to
struggle and is very low energy when we get to no name harbor. I
think he got sea sick or at least stressed out. He uses these
moments to shake and look pitifully so we let him hide in the cabin
instead of outside.
2/8 Thursday we hang around No
Name harbor and as Cheryl walks Thor, I take the windlass
motor cover off to see why it is balking lowering the chain. No
obvious issue, so more work is needed. I also sand the Star engine
pulleys and tighten the belt that is on it now (new a few weeks
ago). If this belt does not hold, I will put a NAPA belt on as that
is rocking on the Port engine. We then pumped up both paddle
boards and played some. Thor jumped in and swam. Drinking a
chunk of salt water resulted in some digestive issues, but he seems
OK. Overall, a good play day for Thor, and us as the weather was
very pleasant.
2/9 The wall on shore is good only at high tide in No Name harbor
(otherwise have to lift Thor out of the dingy, which neither he or I
love), so we head out around 6am, which is high tide so I can get
him a quick easy walk in the morning. Many of our decisions are
based on Thor, I hope he appreciates it!
After we left No-Name harbor we had a spirited sail down the keys
to Tavenier Key (about 50 miles away, and the first spot with even a
little protection from and East wind.). We sailed fast with just the Double reefed main and Genoa
out. and averaged over 8 knots for a few hours. End up
stopping at Rodriquez key, sort of in the middle of the ocean it
seems, but the swells cause no issues when anchored in the cat, and
only modest ones in the dingy. The solar was working great on
the sail down, kicking in around 18 amps for the batteries, which
was nice. Not great access to shore for Thor, so we will head out in
the morning. We found a gap in the mangroves, but very limited
places to walk.
2/10 Head down for an even
faster sail to Molasses Key, but this was a tight fit, no
beach (washed away in the Hurricane) and hard to get ashore. This
combination of issues caused us to pull up anchor and dodge Crab
pots for 6 miles dead upwind back East to Marathon. We anchored
outside Marathon and tried a few ways to get Thor ashore, finally
lifting him on to the dock/wall of an RV park, where a few of the
folks were nice.
Our love of the Keys is in doubt as there are not many spots to stop
that offer any protection from an East wind, and the spots to stop
are not optimal in any event (if optimal includes beach access for
the dog, or swimming etc..). It is interesting, and we are glad to
have checked it out some. Having checked it out, we will likely just
go outside on the gulf stream and skip the whole thing on the trip
back.
There have been some interesting and pretty spot, if you did not
want/need shore access for the dog or walking around.
2/11 Hung out at Marathon in the anchorage outside the key. We are
too tall to get into the harbor itself, so we dingied in.
Marathon is a big destination for many, with 200 plus boats on
mooring balls in the inner harbor, never leaving all winter. It was
a couple mile dingy ride in for us to check it out (we are too tall
to get under the power lines guarding the harbor entrance, so we
would not fit even if there was a spot, but the wait list is weeks
long for a can). Once we got in, we did not see the appeal, as there
did not seem like much to do. But it is fairly cost effective to
stay for a few months on a can, and pump out boats come to you and I
think people just park there all winter.
Thor had nothing but problems when we got him to shore, leaving a
bit of a surprise in the parking lot that was not possible to pick
up. Not much that excited us about the harbor anyway, so I doubt we
will be back anytime soon! We did take the opportunity to go
in for lunch at a spot right on the main channel. Lots of greasy
fries and a good burger for me, some sort of Shrimp burger, fries
and Key Lime pie for Cheryl. There is considerable hurricane damage still
around and the place is pretty packed.
It is fairly windy and a little wavy at the anchorage, but we ride
pretty comfortably.
I spent some time working on the Star engine belt, but despite best
efforts, I could not get the exact same belt that barely fit on the
port Engine on the Star engine. Back to the old (10 hours of use)
new belt, but now with sanded and polished pulleys.
2/12 Went down to Bahia Honda park and anchored between bridges. The
water in the boot alarm was going off again, so I took out the
cabinet to get at the alarm and jammed it full of paper towels and
taped it shut. This silences the alarm, and all other alarms, so we
need to be watchful, but the false buzzer made the engine a holy
terror for Thor (and we did not love it either..)
In interesting spot to get to as you go through a gap in the old A1A roadway
to a spot between the bridges. Had to use two tries on anchoring as
we ended up too close to a mooring or lobster pod thing on the first
try. Anchor held firm for two days despite reputation for very bad
holding. We hit a snag when we tried to bring Thor ashore: the park
was closed to all boat access due to repairs from the hurricane. The
little harbor is blocked off, the other small bay has one boat on
the wall (the volunteer who we talked to), and no one is supposed to
enter the park by boat. Anchoring is fine, but no landings. We
talked to Mike, the friendly volunteer and he said he had ridden out
the hurricane in the little bay. His boat mainly made it OK, his car
was totaled due to water up to the windows from the surge. The
harbor needs to be dredged and there is a boat on shore that needs
to be removed. Overall, he was not sure when things would be back to
normal operations. We did find a spot around the working A1A bridge
where we could let Thor off in shallow water and he could walk to a
little area by the road. This allows the site to work for us so we
decide to stay.
Brief swim in the afternoon and more great weather as we enjoy sunny
days and reasonable nights (maybe 70 at night?), with solid East
winds of 15-20 that have been blowing the last three weeks at least.
2/13 One more sunny clear day and we do a few boat projects (I
install a 2 port USB plug in the Nav station and Cheryl gets a few
more areas cleaned up). Cheryl takes a nice walk around to explore,
this time we leave Thor behind. He attempted yesterday's walk, but
his winter coat is better suited to the 28 degree nights we saw in
St Augustine than 80 degrees and hot sun. He was getting over
heated. Cheryl got a nice shot of the boat,
and we also had a nice sunset
to enjoy. Not much else to report, a nice lazy day overall.
As an overall note, the weather has been great since Kathy left.
When she was here we had lows in the high 20’s at night, typical day
since then has been 80 for the high and 70 for the low. Nice, sunny
weather with an East wind at 15 or so that has been blowing since we
landed in West Palm Beach Jan 24th, so three straight weeks of East
wind with the forecast for more east winds as far out as they go. No
rain since we launched on Jan 11th, so I guess it is hard to
complain about the weather.
2/14
We left in the morning, and bravely headed to Newfound Harbor. I say
bravely as the channel into it is narrow and the charted depths are
5 feet in spots and we draw 5 feet.
This was the only stop possible between us and Key west, so we tried
it. I noticed we seemed very slow right out of the gate heading down
there, we were seeing 4 knots with the Genoa and I thought we should
be getting 6 easy. Both engines were spinning so I did not think we
had a crab pot, but a hour or so later, I noticed a trap being
dragged behind the boat. We had caught one on the rudder, not the
prop, but it was caught and not going anywhere. We dropped sail and
were able to cut the trap free, but the rope and float were still
stuck between the rudder and the hull. After some futzing around we
were able to get a line on the cut line and I pulled it forward as
Cheryl swung the helm. This maneuver took off a little bottom paint,
but we did free the float.
With our prize in hand, it
was photo time!
The bucket was to wash all the bottom paint off the deck that we
picked up from the trap maneuver. With both props clear, and still
more conviction to ride the gulf stream on the way back and avoid
lobster land, we navigated into Newfound Harbor. It was shallow as
advertised, we saw 5.4 feet a few times on the way in, but we did
not ground the boat, and are anchored in a reasonable spot. We have
not tried to get to shore, but hopefully one of the spits of land
will have a spot for Thor. They also look somewhat hurricane
damaged, so the walking paths etc in the cruising guides might be
gone at this point. The Hurricane hit this area pretty hard.
Overall, we continue to add things, the project list is slowly
shrinking, and the boat is rounding into shape. After 6 or so hard
fought battles with the engine belts, I think this is stable, and
the drives seem not to be leaking very much, which is also good
news. The weather has been great, the company outstanding, and we
are getting some more in a week. I think the shallow nature of the
keys and the general lack of beaches one can visit by boat, make it
a little tough with the dog. It is a very pretty spot, and if you
had a small boat with a 3 foot draft, I think there would be tons to
explore. Our mast height and draft limit us some.
We dingied around some in the afternoon and there was a small
channel that was like a small version of Ft Lauderdale, with a
number of cut offs, and boats lining each branch. All smaller boats
to fit the area, but seemingly every house had a boat out
front. We also took Thor to a small island a 1/4 mile away,
where there was a barge/houseboat type set up just off the beach
area. The Dog (lady) on that boat came to the Island to say hi to
Thor, and when Thor got into the boat to leave, the dog jumped in
our dingy as well. The owners called it and it finally jumped out
and swam to the houseboat and climbed up some steps in the water to
get home. A pretty spot, and we plan on hanging around a few days.
2/15 We enjoy a lazy day at anchor. No need to move the boat as we
have a week to get to Key West, and this spot is nice enough. There
is a little beach for Thor, and it is quiet, sunny and great
temperature wise. Cheryl does some morning yoga and I do some laps
around the boat for exercise. Also hang up the remaining two shades
Cheryl made so all the cabins have privacy blinds.
We work some on the boat, with Cheryl polishing the rails, and I
waxed 1/2 the Starboard hull.
2/16 We have a repeat of Thursday, just calmer winds, so I wax rest
of Starboard side and Cheryl does more polishing... It looks great.
We also take longer paddle board rides.
2/17 Saturday, we head off for Key west. 6 days ahead of when we
need to get there, but this will give us a chance to check it out.
We have a smooth motor and sail (we sail with just the Genoa for a
couple of hours at 3-4knots... Lazy crew, I did not bother with the
chute even though it was near dead down wind..). We pull into
the marina and get 50 gallons of Diesel, and also fill our water
tanks. Now Cheryl and I can be pigs until we hit the slip in 6 days.
We also saw the open 40 "Longbow" which is a GLSS owned boat,
hanging in a slip at the marina. I also saw them last Feb in the
yard at Cracker Boy, and in DeSable Harbor before the start of last
year's solomac. We did not like the free anchorages, so we went
around to Key West Garrison Bight marina where there is a mooring
ball field. We get a ball with me in the dingy and Cheryl driving,
works pretty well. The ride to the check in is 15 minutes, but there
is a nice island nearby for Thor. We will explore Key West on foot
tomorrow and leave Thor to guard the boat...
2/18 Sunday. The morning was spent dodging some light rain and
rigging up the lazy Jacks for the main (the parts I could use
anyway, the bulk of the line is too thick to go into the mast, but I
was able to redo things so I could use the lower portion). I also
took some of the excess new lazy jack line and created custom bumper
lines for all 8 fenders, so these now look ship shape. A few other
small jobs and after Thor's noon walk, we headed into town. It is
about 1.4 miles to walk to Duval street and we found a good Mexican
place to have lunch, and generally headed back.
The winds have picked back up and it is a steady 20Knots or so from
the East. The Dingy generally keeps us dry in the chop.
2/19 Monday. We Stay put and I mess with the engines again. I manage
to force the NAPA (OEM Sized) belt on the Star engine, but after 30
minutes of running it is still bar tight, so I remove it and put the
old/new one back on. Too tight will destroy the bearings in the
water pump and alternator, so I will wait for the parts Tom is
bringing down. I also replaced the impellers on both engines. They
were the right size, but not the OEM part as they did not have the
clever screw in extractor point on the end. The Port engine is
gaining a little water in the sail drive. Not a ton, but some, so I
will drain a little off and move on. I also cut off the excess rough
fiberglass from the half done repair job in the port engine room,
and sand it down and put White Gel Coat over the repair. This looks
better, is smoother, and I can paint the gel coat gray if I find a
good paint match down the road. We took Thor in for a noon swim and
let him get some exercise. He did pretty well not drinking the
water, and so we should be able to let him swim more as we go to the
next stops.
2/20/2018 Tuesday. One more very windy day and we decide to head to
town. The pin on one of the
dingy davit blocks had broken off so I had to use the hacksaw
to cut it free and replace the shackle. That was it for the exciting
boat projects for today. Town
being the big adventure, with this tour being lead by Cheryl.
We saw a pretty cool art boutique with some very fancy items
(prices, not on display..), and got a couple of scoops of Ice Cream.
2/21 Wednesday. We took a three mile hike to pick up the head motor
and base from the UPS store, and on the way there saw near heaven,
with a 5 guys burgers, a Denny's, a Dominoes, and a few other fine
dining establishments. As it was too early for 5 guys burgers (not
for us, for them..) we had a nice meal at Denny's. We also picked up
a couple of other items on the way back and turned in our dingy dock key. Glad we
have the larger dingy as it makes the ride back and force a lot
easier and drier. After we got back we took Thor for a afternoon
swim, which went well and he seems to not be drinking too much
water. Thor has made himself at home on the boat, which is
very nice to see. The Solar is working very
well, and if it is a clear sky day, we pretty well keep even
for the 24 hour period with our 450 watts of solar. We got a
great call from Matthew and Angel at night letting us know we are
going to have a Grandson, which is pretty exciting!
2/22 Thursday, our last full day on the can for this round, and we
spend it attending to odd jobs to get ready for company. Some
cleaning of the rubber rail around the cockpit as well as stowing
items we are not installing right now like the SSB help get the boat
a little more ready for company. The morning started out rainy,
which was our first measurable rain since Jan 10 or so. it soon went
away, and the winds returned. We end up with a very pleasant sunny
day. I also got Thor some more swimming time on what is his favorite
beach so far! He is still trying to sneak into the cabin,
but we are holding firm!
2/23 Friday, we headed to the slip in the Key West Bight Marina. We got in smooth and started
the clean up process. Even though we docked smoothly, as the dock
hand pulled us forward, we got some gel coat scratches from some
nails on the pilings.. Hard to keep a perfect hull!
I got 10 gallons of dingy Gas, and we did some clean up before
everyone arrives this afternoon.
2/24 Saturday, we sent folks out in multiple directions to get food
and drink, propane, and other items for the week. We also tackled a
few other jobs like replacing the alternator belt on the Starboard
engine (hopefully for the good now..), and changing the gear oil in
the outboard. Also picked up a few supplies at West marine. The
fresh water pump was sounding funny and this turned out to be it's
final sounds.
2/25 We left the dock around 6am Sunday to make the run down to Fort Jefferson. We left the
dock smoothly despite a breeze pushing us on, and boats in front and
behind, which was nice. The sail
down was a nice down wind ride with Lobster pods, the whole
way, but also Dolphin's
and turtles and lots of Man-O-War jelly fish. A pretty nice sail overall, and
we got in around 3:30 or so. I took some time on the crossing to
replace the fresh water
pump, which at this point had quit completely (12 hours from
sounding funny to dead..). This was a little tricky as the
replacement pump was not identical, and the wiring to make the panel
light go on took a second to figure out. After some futzing, it was
in and running, and it is quieter than the old pump, which is nice.
Once we got there, we immediately took Thor to shore, but to
the wrong shore and had to get him back in the dingy as the area was
a bird sanctuary. Once we learned the rules, we did better!
2/26 Monday was spent exploring
the fort and doing some paddle boarding. The Fort was
interesting and we spent a number of trips visiting it. The few guns they had left were
fairly cool to check out. There were also two sea planes that made
regular runs to the fort and a ferry that took people from Key West
each day. Some of the team snorkeled around the fort, which was OK,
but not outstanding in terms of the snorkeling. The weather was
great as usual, the water warm, and the company outstanding, so
it is hard to complain.
2/27 Tuesday, we headed over to Loggerhead Key and did some walking
and snorkeling. It was pretty good snorkeling and the island was
nice. Thor was very unhappy when we all left him, but he did get
over it.
We went back to Fort Jefferson for the night and the anchorage
filled in a good deal with 12 boats in the anchorage by the time
they stopped arriving. We helped one power boat who did not know how
to anchor (mostly in self defense), and Tom was able to get a baggie
of Ice for the evening drinks for our trouble! One routine was to
get Thor ashore three times a day. It allowed for some peaceful evening walks around the
Fort. We also had a nice spot to park the dingy each time.
2/28 Wednesday we headed back and despite the earlier weather
forecasts, we had to motor into a bit of a breeze. We stopped at
Boca Gande Key and anchored for the night. It was a pretty enough
place, but not super interesting and so we pushed back to Key West
the next day.
3/1/ Thursday, we sailed and motored back to key West and took a
mooring ball in the main city mooring field. After checking in and
getting squared away, we took a walk into town and poked around
before enjoying our final
dinner of the trip.
3/2 Friday was clean up and packing day and the weather was great,
with light winds and no waves in the harbor. This made the 1.5 mile
dingy ride to shore dry and easy for the folks flying home. It was a
great week with Doug, Sarah, Tom and Heidi. One could not ask for
more helpful and easy going shipmates. Friday night I spent some
more time looking for the water leak in the Starboard hull. I traced
it down to a leaking pipe going into the water heater under the aft
bunk. After some work, I was able to replace the pipe and this seems
to have stopped our water issues on that side! I think this was also
freeze damage, and I will drain the system from the two water
heaters next year, as I know for a fact that tons of water comes out
when you open this fitting!
3/3 Saturday, Cheryl and I spend 3 hours walking around Key West. We
covered the areas we had skipped so far, like the cruise ship dock,
and some of the other attractions. It was a windy day from the NE, so a
little cooler which made the walk very pleasant (as well as the
company). It would have been a wet ride in the Dingy for folks going
to the airport, so we lucked out there.
3/4 Sunday was a modest work day, with some gear oil changing for
the leaking saildrive, pinning the boom vang, and working on our
Taxes being some of the highlights! We also gave Thor a nice swim to tire
him out for the lazy/low exercise days ahead. Thor has figured out not to
drink the water, so his swims have no bad consequences. The
mooring field is good in many ways. Everything is far away, but you
can get to everything. The island
we walk and swim Thor on is typically empty, so we have the
place to ourselves. The dingy dock in town is nice and secure, and
the walk into Key West is not bad. As one review said: "Everything
is 1.5 miles away, the dingy dock, Key West downtown". It is all
workable, and not a terrible place to stop.
3/5 We headed over about 11am and docked fairly smoothly into the slip in Key West bight marina.
It was a tight turn with a cross wind, but overall, we made it
pretty smooth. The boat next to us was one I remembered from the
2012 Salty Dawg rally. Always a small world. We were very efficient
in our task, spinning up 4 loads of laundry, getting groceries, some
gas, a new fresh water pump (so we are back to having a
spare), and then wandered off to see a movie and have
dinner. Very efficient dock day.
3/6 Tuesday was the day to push on. We had a nice one day weather
window for a fairly smooth sail up to Miami. Although the goal is to
avoid the overnight trips, we were both happy to stop dodging crap
pots and avoid a upwind motor in Hawks Channel. Plus there were not
a lot of good spots to stop if we wanted to break it into a few
days. None of the stops on the way down were "must see" stops for
the way back. With this in mind, we filled the water tanks, and the
bladder tank, so we were at full water, and headed out around 11am.
The ride started out pretty sloppy, but after a couple of hours
things settled down some and we were able to sail. There was a nice sunset, and the
boat sailed very nicely. With about 70 degree apparent wind of 12 knots we were
getting 8 knts of boat speed, which was nice. As night
fell, I noticed the bow running light was not working. Cheryl and I
worked on it and got it going again, but the light fixture and bulb
are both iffy at best, and the new bulb I bought I could not get to
fit in the light socket as it had been damaged or in some other way
messed up. Time for a nice LED light up there and be done with it.
Ended up sailing about have the 130 miles and motor sailing a chunk
more. Overall, a pretty nice sail and passage, a great moon rise,
and with our arrival as planned at around 8am into Miami's Biscayne
bay.
3/7 Spent the day off of No Name harbor. There was room in the
harbor for us to anchor, but we liked the space and breeze outside.
By timing our trips to shore we made it so Thor could jump from the
dingy so no lifting was needed. Both Thor and I liked that!
The area is a park, and there were nice trails for Cheryl to walk on
with Thor so everyone could get some exercise.
3/8 Took it easy with some small boat projects like patching the mainsail cover
which we had torn on the solar
heading down to Fort Jefferson. I had tried a few things, but
finally used the hot canvas cutter to melt the tear some, and cut a
few scraps from one of the hatch covers Cheryl had made. With these
I sewed a patch over the inside and then Cheryl sewed a nice patch
over the outside, covering my stitching, and making the whole thing
generally match. I hoped to install new screens for the port aft
head, but the new screens were not a exact match and so the fit was
off. I also discovered the headliner was not set up well to screw
the screen into. Fixed this
and was able to tweak the old screen to get it mainly working, so
after these repairs, I put the old/fixed screen back up. It
was fairly windy overnight, with a nice chop, but the Cat rides this
sort of thing well, and anchor is rock solid, never moving an inch.
3/9 Fairly easy day, windy but pleasant. Took the time to clean the
davit winches as one of them was sounding odd at best. The center
spine that the winch handle is attached to was hard to get out and
had some corrosion I had to polish off. I think if I let this sit a
couple more years, they would be frozen up. We also locked in haul
out date, and made some final plans for the end of the trip.
3/10 Saturday was looking like a good weather day to head up to West
Palm Beach, about 60 miles away. We followed the usual routine, with
me taking Thor in before sunrise for a quick walk, and got the
anchor up as the sun was starting to get 6am start to West Palm
Beach. We saw a great
sunrise as we headed out, and then had a fast ride North. Peak
speeds we saw was 12.8 knts, this had a 2 knot gulf stream push, but
we were doing well. Averaged almost 9 knts for the trip, and arrived
around 3pm at West palm. Sailed the whole way with a reef in the
main and full Genoa.
3/11 Took a lazy day working on some of the odd jobs on the to do
list like polishing the blocks and shackle fittings on the
boom, and took a long dingy ride to the anchorage between the
bridges. Glad we did that as they are setting up docks for the Palm
Beach boat show at the end of the month and the public piers are
closed down. It would not have been a great spot for Thor with no
access to shore! Quite a production to set up for this show, with a
lot of docks being put together, a large tent and massive power
being run so all the boats can have the AC on :-)
3/12 There was a front coming through today with a strong cold front
behind it. I Cleaned a mast winch before the rains came and then we
checked the boat for leaks as it rained. We looked pretty good on
the leak front, with a couple of small leaks to chase down, but now
some ideas of where to look! After the front came through we sat on the bow and enjoyed
the 20-30 knots of breeze
post front.
3/13 Finished cleaning
winches, put stuff on hatch seals, puttering puttering. Cool
day after the front. Now nearly a north wind and maybe 60 degrees.
Nice and Sunny though.
3/14 Wed, did some cleaning up, and made it so I could see the Nav
station desk for the first time all trip.. Mounted the AT130 antenna
tuner for the SSB, and worked a few other small projects. Cheryl
came below as we were enjoying a well earned drink enjoying the sun
drifting lower in the sky, and asked “Mark, did you spill something
down here?”
My first instinct is “gee, I hope not, what does it look like”
(because you never know what I might have spilled…). I came to check
and there was a lot of water running on the floor and the water pump
was running. A quick check under the sink got me soaked. OK, not a
slow leak. It turned out the hot water line into the sink had burst.
Lucky for me, it was all rusty and very hard to reach, and hard to
see what you were doing as it was behind the sink.. Cheryl was
not able to keep the faucet from rotating with the pliers when I was
trying to turn loose the rusted nut holding it to the counter, so I
put a hand clamp on the end of the adjustable pliers forcing it
closed tight. We were able to get it out and I was able to cap off
the water lines. Had to use the Sea Gull to wash dishes tonight.
3/15 Spent some time after the morning walk thinking about the
faucet issue. Not clear how easy it will be to buy something today
that looks and works OK. After a few other ideas would not work, I
took two good feed lines off the sink in the bow “slave” cabin which
we never use. Put things back
together with the new hoses and now the stupid thing leaks
very slightly at the joint in the fixture. Must not have liked the
gentle way I removed it! It is back in business though, and so we
are going to look into longer term fixes down the road.
3/16 Friday, exactly 4 weeks and we should be in Newton, three weeks
till we haul the boat, so the trip is winding down. We take
advantage of fairly calm weather to head north to Ft Peirce. Lake
Worth is flat calm at night, a first for us, and the dingy ride in
at 6am is a smooth motor over a fairly calm lake. We get the anchor
up and are on our way around 7am. The Ocean is fairly calm as well
with a light NW wind, so we are motoring in the calmest waters we
have seen the whole trip. Maybe 1 foot waves, maybe a one foot
swell. A day would not be complete without some mechanical
issue. Today's was the port engine would not turn over when I hit
the starter. Not sure if the switch is bad, the battery weak, or the
starter connections dirty (although the starter is new this fall,
and should be OK). Need a lot of tools and skills to maintain this
boat, but I still like it overall. We have decided we will not buy
such a used boat in the future. Too many weird items have needed
work.
We get in around 3PM and anchor in a spot off the channel north of
this little Island. I don't love the spot so we pull up anchor and
as we do, the Coast Guard is heading our way. They don't say
anything, but just hover about 5 feet away as we pull up anchor and
as we head back out the channel. I try to call them on the radio. I
get CG in Miami, I tell them I am trying to reach the CG boat about
5 feet off my port stern, they say OK, but the local boat still does
not answer. After 5 more minutes of this weird stalking, they come
tight along side and ask to board. We tie up Thor and they do a
inspection, which we pass. Seems very odd behavior, but not much we
can do.
We go back and anchor on the south
side of the island and get Thor ashore for a little romp.
The Island is pretty nice for this and Thor gets a well deserved run
on the beach. Some of the
beach comes and goes with the tide, and it is very popular,
getting packed with small boats
and people during the day.
3/17 Saturday, We Stay there and the boat rides the current switches
very well. The Island get very busy during the day as people set up
tents and generally make a day of it. We take an exploratory dingy
ride around, and I also re-attach the main ground on the port
engine. Still is a little flaky, so I am thinking it is the starter
switch going bad. Overall, a very nice day and we enjoy the place. I
also tore out the weird sticky caulk in the port aft cabin around
the far back port, and re caulk it. I had earlier caulked the
outside trip piece. Hopefully this solves the leaking we saw there.
3/18 Sunday. Looking at the weather there will be a strong front
coming through Tuesday and one mid day Monday, with some strong
winds for Wednesday. We decide to make the slip in Daytona for a
week and head out Sunday afternoon to sail overnight and get to
Daytona ahead of the weather and at high tide for the channel coming
in. Around 3pm we head out and since we have plenty of time to make
the 110 mile trip, we sail in fairly light air the first 9 hours or
so. We put the Chute up for a
while and generally enjoy a very nice, quiet sail. There
are some Dolphins and the Ocean is pretty smooth. Thor even comes up
to enjoy the sail.
3/19 Monday. Around 1:30am the winds go aft and die some more so we
fire up the engine (starboard this time) and motor planning to
arrive right about 9am. About 7am I spot lightning and the weather
radio and radar show a line of thunderstorms coming through. We are
basically around 6 miles from Daytona, with only two drift net
fishing boats around, each about a mile away, so we kill the engines
and wait to let the front hit
us on the Ocean rather than as we snake our way up a
unfamiliar channel. This works, and after a medium strength
thrunderstorm and rain, we push on in. There is a second wave
coming, but except for some rain, we get docked before it hits. This
weather was not forecast, nd even in the middle of the night the NWS
was not calling for anything in the morning. Always need to be ready
I guess.
The way in is interesting, and our first taste of the real
intercoastal. We see many dolphins and a few spots of shallow water.
The tide is 3 feet and without high tide, we would have been pretty
close to grounding in a few spots. The dock is nice and the
area is quiet. Seems like a nice change and we will enjoy spending a
week here.
Cheryl and I enjoy a evening cocktail as we watch the second wave of
rain and storms roll in. They we head off to dinner in the dockside
restaruant nearby. It is raing hard when we come back out, but that
helps show my aft cabin port fix worked.
3/20 Tuesday we spend puttering on the boat as there are waves of
strong storms coming through. There are a few tornado warnings, but
the weather that hits us is not that bad. It seems the worst of it
went just south of us. We do a short dingy ride around the area, and
run the fuel out since we will not need it for a little while. Get
set up with a rental car for Wednesday and also discover the main
salon AC unit is not working. After swapping out the control board
on the AC panel with no change, we order a new main AC control
board, which should come Wednesday. Seems like something needs
fixing every single day :-)
3/21 Wednesday we grab the rental car and get resupplied. Groceries,
some plumbing parts, a nice dinner out and a trip to visit the truck
in St Augustine are some of the highlights. It is very windy all day, 20-25
knots, gusts over 30, 2 foot chop in the small little harbor
here. Nice to have the
big bumpers! Cheryl tried to take a morning shower, but no hot
water on Starboard side. Lucky for me the port side was still hot.
The water heater turned off and then did not turn on as needed when
the water cooled. I turned it off, then on at the main panel and it
fired back up. Always something! I took the opportunity of a
cool day pinned against the dock to wax the port side once more. I
did it when we were in St Augustine, so now it has two coats, which
it needed. I did the Starboard side at newfound harbor, so hopefully
that helps.
I put a new battery in the truck (which was a pain), and hopefully
things are ready now for when we come up.
3/22 Thursday, Roger and Eileen come..
I worked on the AC unit. Cheryl worked on the canvas. We are looking
at the weather and leaning towards heading out on Saturday.
AC does not quite work perfectly as the temp sensor seems out of
order. I need to putter with that as well. My truck key was cracked
in half and falling out so I epoxied that back together. Seems the
dealer would need to reprogram the car anyway, so locking up this
key is no big deal. Just can't ever replace the battery!
Cheryl's folks come on time, and we are joined by old neighbors from
their days in Indianapolis. Makes for a nice visit and a enjoyable
dinner. Thor uses the time to
rest up.
3/23 Used Roger's car to get parts from West marine and got his car
oil changed. Generally puttered around all day...
3/24 Due to wind forecast for later in the week, we decide to head
up to St Augustine today, with a 7:30am start. Low tide, but what
can you do. We go slow over the couple of real low spots, but never
see less than 6 feet at low tide. Always pretty on this stretch of water.
Smooth ocean, makes for a nice motor. Roger and Eileen get a
little Ocean voyage of 55 miles or so and we are happy with choice as the
weather Sunday was not the best.
3/25 Sunday Spent day basically getting the car up from Daytona.
Left on 10am tender and rode back on the 4PM tender so basically an
all day affair, but things went smoothly.
3/26 Monday 10am tender takes Roger and Eillen ashore and we dingy
in to send them off. A nice visit, with no issues and I think
everyone was happy to get some Ocean sailing (well motoring...) in.
With a day at a dock, a day underway, and a day at the can, they got
a taste for everything but anchoring! Spent the day getting some
things organized, and dodging the rain that fell most of the day.
Also, after three other meathods, I came up with a solution to
tieing the can that prevents it from scrapping the hull and taking
off all the bottom paint when we are wind against the tide. I tied
it short, back to the windlass cleat so there is not enough rode
left to reach the hulls. Seems to do the trick.
3/27 Took the day puttering. Gave Thor a long walk to the garage and
back, and caulked one of the heads.
3/28 Wednesday. Wake up to a clogged port forward head. Called in
time to get the pumpout boat so the tank was empty. Spent a few
hours getting the hose off the tank end, and cleaning the calcium out of the
hose. Lots of it had broken loose and clogged the hose from
the head. Put things back on, and noticed the 1.5" hose to the tank
was leaking at a small tear where it hit the tank fitting. This
might have been there already as the hose was oddly pushed up and
that might have been to move the slice slightly up. In any event, I
did not have any 1.5" hose so we headed off to West marine to buy
some. The step down fitting was too big to get the hose over, even
after I sanded it some, and I had to hammer the hose on to get a
reasonable amount on the fitting. Nothing is ever easy! Got it sorted,
decided to date the repair for the record, and the head is in great
shape now. Did some more caulking as well.
3/29 Thursday, we met Kathy for a motor around the area. She showed
up around 1:30 after a visit to Paul and Lori, Lance's Mom, and
Jennifer and Charlotte. It was quite windy so we motored under the
bridge, wend most of the way out the inlet, saw large breakers on
each side, but the inlet was still passable, and came back. The
large dredging machine was tucked back in the inlet some due to the
rough conditions. Had a nice visit and went to dinner around 5pm (we
are the early bird special folks!). She headed back to Orlando, and
we had a rough and wet dingy ride back into a 20 knot wind fighting
the current. Hard to stay dry on that one, and I got nailed a couple
of times when I took Thor in for his end of day walk. The wind and
current produced a fairly jerky motion for the boat as well, and
that made it less comfortable sleeping.
Mary was sorry to have missed the outing, but she was not feeling
strong enough for the trip. We will get her next time!
3/29 Friday. We got some groceries in the morning and I got a new
pair of shoes. Cheryl called them "old man shoes", but I got them at
a sporting goods store in the basketball section.... Who can judge
fashion. We did some shopping and clicked off a few items getting
ready for visitors on Sunday. I put the base part of Cheryl's head
back together and changed the oil in the Starboard engine. Trip is
clearly winding down!
3/30 Tried a new can tie with the painter on the boat, so the can
could not hit. This worked OK, but put a lot of strain on the can.
The next day the harbor guys came by and told me I could not have
the painter on my boat, but I could tie lines to the can as long as
I did not use the splice eye.
Worked on Cheryl's head. The hose to the tank was clogged with
calcium, so I got that sorted, I think the motor is leaking when I
ran my tests, so that is on the replace list as well. Changed oil in
both engines. About 60 hours on each for the trip (estimated for
star engine).
3/31 Re-tied my mooring lines with a line to the can from each hull.
This keeps the ball of the hull and also smooths the ride. Worked
well in the windy period we had against the tide over night. Changed
the oil in the generator and filter. Noticed the old filter was the
wrong size and hard to get off... Oh well. Now all three are
changed. Exactly 100 hours on the gen since launch. Likely a few
more the last week, but not bad. Spent a chunk of time finishing our
taxes on Turbo Tax, so it should be ready to run when we get home.
4/1 Sunday. Fixed the salon AC issues in the morning ( I had plugged
the thermostat into the wrong spot when I replaced the control power
board). Used the last of the Caulk to do much of the starboard
heads. We then picked up some anti freeze from West Marine and some
containers from Lowes before heading to the airport to get Bob and
Carol.
4/2 Great sailing day. We headed out into a fairly calm Ocean and
got a nice close up of the
dregger they use to keep the channel clear. We went out about 8 miles,
and enjoyed a near perfect
sailing day. We had some fun getting going as the Starboard
engine start switch would not work. I was able to short the starter
to get it working and rigged a temporary switch to start it until I
got things figured out. We stopped at the Fuel dock and filled both
water tanks, and took in 85 gallons of Diesel. Very good and
productive day overall.
4/3 We took advantage of the fairly calm weather to remove the
mainsail and cover. It took about 90 minutes, which I viewed as
pretty fast!. We then headed to shore for a trolley ride to explore
the town and take a trolley tour. Retied the can again, this time
with 3 strand lines run through blocks on the ends of the hulls.
Gives me better adjust-ability and shock absorption. Seems to work
great, but need to un twist them each day due to the tide swing.
4/4 Everyone else went on a lighthouse tour, I worked on the engine.
No success. I could not track down the starter issue or the blower
issue.
4/5 Thursday, not one to give up easily, I spent a good deal of time
removing the engine panel, cleaned all engine wires and got the
starter back working. Wired the hour meter to the fuel lift pump,
got this working as well. After a nice lunch, we headed into town to
walk around, and visit odd spots like the museum of weird junk
collections! We had some weather blow in, and threaten us with heavy
rain, but all we really got was a very cool cloud formation and
sunset.
4/6 Friday was our last day in the water, so we made use of the
mooring field's free pump outs and got both heads pumped in the
morning. Took more small items off and at 1PM, we headed to the boat
yard to get hauled out. This went
very smoothly, which was nice, and by 3:30, we were blocked and it was
time to take Carol and Bob to the airport.
4/7 Saturday was a busy day packing the boat up, and also our last
night sleeping on it for this "trip". Much of the time was
spent doing laundry and putting the engines to bed. Good old Thor
spent these last two nights in the car, which he seemed OK with.
4/8 Sunday. We finished the packing of the boat, put all the bunks
on their sides, covered all hatches and in general, tuck the boat
in. We hopped in the car around 12:30 and we were back in Newton at
3:30 the following day, after a 8 hour stop at the midway point for
some sleep.
This ends the exciting story of our quest to conquer Florida. As
with many endeavors, I feel the safest path is to simply claim
victory, and sight a few meaningless stats to prove the
point..
- We had 22 guests this trip, 14 of which stayed overnight.
- We covered 1160 NM on the trip,
- Spent 92 nights on the boat,
- Put about 60 hours on each engine and 101 on the generator
- Spent 38 nights at anchor, 4 nights sailing, 12 days at slips, 28
days on mooring balls, and 7 nights on the boat while in the Boat
yard in dry dock.
We never were arrested, and the only time we were boarded by law
enforcement, they found nothing wrong. No one was seriously hurt,
and we never ran aground, hit anyone, or dragged anchor… With the
many great guests who honored us with their company, and the good
number number of wonderful sails. I say victory is ours!